09-29-2018, 10:58 AM | #1 |
Drives: 2015 camaro 1le Join Date: Jun 2015
Location: pasco wa
Posts: 233
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P0305 code
So I went to the strip last night and got 3 runs in and on the way back I got the service stabilitrak and cel. Pulled the code and it says p0305 and cel is flashing. Swapped plugs and it came back on again. Swapped plug wires and it came back on. Lastly I swapped coils and it still came back on. Any ideas what to look at next?
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09-29-2018, 12:04 PM | #2 |
Drives: 2015 camaro 1le Join Date: Jun 2015
Location: pasco wa
Posts: 233
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Just pulled the valve cover and the #5 intake rocker was loose and I pulled the pushrod and it was perfectly straight. Reassemble and codes went away. I think I dodged a bullet
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09-29-2018, 07:58 PM | #3 |
Ponies are for girls
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Sounds like it. Nice job!
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H&R 1.8/1.7” drop, Overkill 80mm + intake ported by AFS, 1" insulator MACE, Accel Super Coils, THR cai, JET MAF sensor, Hurst shifter handle, GPP strut tower brace, CI ice cube tray hood vents (functional) @SemperFiCamaro
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09-30-2018, 08:28 AM | #4 |
old school chevy rodder
Drives: 2013 2SS/RS Manual,DM exhaust,CRT Join Date: Jul 2012
Location: Oregon
Posts: 5,587
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Hope you carefully inspected the Trunnion , its not normal for one rocker to walk itself loose...……….
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09-30-2018, 08:40 AM | #5 |
corner barstool sitter
Drives: 08 Mustang GT, 19 WRX Join Date: Jul 2012
Location: Eastern Time Zone
Posts: 6,990
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Keep an close eye out for further loosening, which could mean that the stud is pulling out (unscrewing? not sure what kind of studs are used). Or worse (cam lobe & lifter).
Norm
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'08 GT coupe 5M (the occasional track toy)
'19 WRX 6M (the family sedan . . . seriously) |
09-30-2018, 01:32 PM | #6 |
Drives: 2015 camaro 1le Join Date: Jun 2015
Location: pasco wa
Posts: 233
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They are the stock studs. Didn't notice the trunion loose at all. The head didn't appear to be stripped either. Was able to torque it back down. I may pull the valve cover and look again but I did think it was weird that it came loose.
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