05-22-2015, 08:58 PM | #15 |
Drives: 2014 2SS M6 "CHRISTINE" Join Date: Mar 2014
Location: Boston Metro North
Posts: 2,916
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I don't know much about the VTC but why have substantial mods with no tune?
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Mods: ARH headers and hi flow cats, VMAX ported throttle body, CAI air intake, Slowhawk Performance tuning |
05-22-2015, 11:38 PM | #16 | |
Drives: 2018 1SS M6 Join Date: Nov 2014
Location: Houston
Posts: 2,617
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05-23-2015, 12:02 AM | #17 |
Too much is never enough!
Drives: AGP TT SS [COTW] 4/20/15 Join Date: Feb 2014
Location: Toledo,OH
Posts: 4,149
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First I've heard of it, there seems to be a lot of misinformation out there, contact Ahmed, he will tell you its ok to use all settings. EC 1-7 and SP 1-9.
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05-23-2015, 03:14 AM | #18 |
Lurking in my SS
Drives: '14 2SS/RS L99 Join Date: Jul 2014
Location: Louisiana
Posts: 290
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05-23-2015, 03:19 AM | #19 | |
Lurking in my SS
Drives: '14 2SS/RS L99 Join Date: Jul 2014
Location: Louisiana
Posts: 290
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05-23-2015, 03:23 AM | #20 |
Lurking in my SS
Drives: '14 2SS/RS L99 Join Date: Jul 2014
Location: Louisiana
Posts: 290
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IM JUST WONDERING HOW DID PEOPLE FIX THIS ISSUE BEFORE THE VTC WAS INTRODUCED. IF PEOPLE WERE GETTING THROTTLE BODIES REPLACED AND PEDALS AND COMPUTERS REPLACED WITH THIS CODE 3 AND 4 YEARS AGO THEN MAYBE OUR CARS HAVE A DEEPER ISSUE. IDK
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05-23-2015, 03:30 AM | #21 |
Lurking in my SS
Drives: '14 2SS/RS L99 Join Date: Jul 2014
Location: Louisiana
Posts: 290
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I HAVEN'T HAD THE MODS LONG AT ALL. I DIDN'T WANT TO GET TUNE AFTER TUNE FOR EVERY PART I ADD SO I WAS WATING FOR A COUPLE MORE THINGS TIL I TUNE IT SO I CAN DO IT ALL AT ONCE. PLUS IM HONESTLY JUST AS FAST AS SOME FRIENDS OF MINE WITH TUNES SO IM NOT RUSHING IT.
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05-23-2015, 07:58 AM | #22 |
Drives: 2018 1SS M6 Join Date: Nov 2014
Location: Houston
Posts: 2,617
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Some one posted a youtube video a short while back about this. The guy in the video checked his TB connector and found a loose wire in it. Always worth checking. He called a tug test, light tug on each of the wires in the connector. Found one that was hanging on by only a couple strands of copper.
Also, try reinstalling the VTC, prehaps the calibration is off. Maybe I'm wrong about the code but it could be related to the ecm reading a difference between the pedal and the throttle body. As far as the tune, I guess it depends on the tuner, but the few I've talked to over the years will do the first wide band to get you set up. Then only charge a nominal fee for additional mods as you go. Of course there are always those little things like fuel pump, filter, injectors that can go south as well. |
05-23-2015, 11:04 AM | #23 | ||
Drives: 2014 2SS RS 1LE Join Date: Mar 2015
Location: St Petersburg, Fl
Posts: 372
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05-23-2015, 11:12 AM | #24 |
The vtc is telling your car one thing and the traction controls are telling it another . I doubt anything is wrong, try putting in competitive mode.
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05-23-2015, 11:19 AM | #25 | |
Drives: 2010 Camaro 2ss/Rs Transformers Join Date: Aug 2014
Location: Yorba Linda, California
Posts: 1,564
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Good explanation. He also told me it was too sensitive for the v8s on higher modes.
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05-23-2015, 12:39 PM | #26 |
Drives: 2018 Redline Edition 2SS Join Date: Dec 2014
Location: Mays Landing, NJ
Posts: 778
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Onstar is clueless, they're very general in their diagnosis. Bad gas won't give you a P2138, it's a correlation code, the PCM is seeing different values from the throttle position sensor and the APP sensor....
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2010 Infiniti G37x Sedan for the DD. |
05-23-2015, 05:50 PM | #27 |
Drives: 2014 2LT RS Join Date: Apr 2015
Location: Canada
Posts: 256
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Last edited by 1Canuck; 05-23-2015 at 06:14 PM. Reason: moved to LFX |
05-24-2015, 02:01 AM | #28 |
Lurking in my SS
Drives: '14 2SS/RS L99 Join Date: Jul 2014
Location: Louisiana
Posts: 290
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Ok everyone. Thanks for all the replies and advice. I really appreciate it. Here is an update. Friday when I posted this I unplugged my battery and let my car sit for about two hours. Also unplugged the controller. Put everything back to normal and turned the car on (didn't start it) and listened for the fuel pump and boom another engine power reduced message and I wasn't even driving. Car wasn't even started.
So I went to the next option. I pulled the two fuses and let the car sit for an hour. Started the car and it started fine with no messages. I ran the little gas I had left from texaco out. I went to shell and filled up halfway with 93 octane and just to be extra I went ahead and added a bottle of octane booster. I started the car and it seemed fine. I even got my exhaust pop noise back. I rode around again for about 10 minutes and the car responded so good. It felt like She got her soul back lol. I even punched it a few times and it responded fine again. My CEL even cleared. It's been over 24 hours and nothing has happened. I'm hoping it was the bad gas or perhaps my gas cap was loose. I don't know. But there is the update for you all. Let's hope it stays fine. I will update yall again later. |
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